Saturday, 21 December 2024

Positive Stops and Final Drive Sprockets

I needed 3 positive stops for the 3 immediate projects – KTT 55, KTT 305 and the Cammy Special. Both KTTs have a 3-speed gearbox and the cammy special will use the 4-speed ‘box.

This is the collection of positive stops and assorted parts that I have.

The one on the top right of the picture is a new-manufactured item that I bought on eBay Australia many years ago and is the only one that I have that will fit the 4-speed ‘box. The backplate, GC-2/2, is different for the 3 and 4-speed gearboxes – the top central hole is in a different place, although I could only find one part number in the spares book.

The other 2 complete positive stops are from KTT 55 and KTT 305. The latter has the wrong mounting bracket but luckily there is a correct bracket in the collection of bits at the bottom of the picture.

The new positive stop had been expertly crafted – a real work of art and superbly manufactured. This, for example is one of the pawls.

And this is the motley assortment of pawls from my old positive stops

and which were all pretty loose in their holes in the main body, GC-21 (referred to as the “Centre Piece” in the spares book – makes it sound like a floral table decoration for a dinner party!).

I decided that I would make some new pawls by copying the new ones that had come from Australia. These need to be hardened steel and so the first step was to order a bar of O1 tool steel of an appropriate size that I could subsequently heat treat.


I then chopped a piece off and after cleaning up the ends, set it up in the 4-jaw chuck in the lathe to machine the spindle.




The nominal ¼” diameter (actually 0.245”) spindle on both the Aussie pawls and my copies is slightly longer than the originals and as the longer spindle fits into my GC-21 main bodies, I retained this feature because I believe it is a better design as the pawl is better supported.

After measuring the angle of the tapered surfaces with a digital protractor


The pawl was set up in the rotary indexer in the milling machine to complete the machining.


After a few hours I had 2 new pairs of pawls – Aussie new ones on the left in the picture below.


These pawls turned out to be longer than the originals that were part of the 3-speed positive stops – 0.82” versus ~0.78”.  While I was making these, I compared a few other parts of the new positive stop with the originals. Interestingly, I found that the 3-speed ratchet lever, GC-22, was different: the picture below shows the new Australian manufactured one on top of an original.


I concluded that whoever made this in Australia redesigned much of the mechanism. Anyway, with the 4-speed ratchet lever fitted, it worked perfectly on the 4-speed gearbox with positive selection of all gears and neutral.

So, back to the 3-speed positive stops.

Before fitting and testing the new pawls, I needed to sort out 2 new linkages that connect the ratchet lever to the Striking Lever, B-65. I believe that I mentioned in the past about the importance of eliminating any sloppiness through wear in the linkage on hand-change vintage Nortons using Sturmey Archer gearboxes – it invariably results in difficulty in selecting or staying in gear. When rebuilding these Velo gearboxes I had found on all of them that the part referred to as the ”striking lever double knuckle joint”, B-69, was badly worn and introduced a lot of free play and I replaced all of mine. This part is (or, at least was) available from Grove Classics.

I also replaced the rest of the linkage: new ball joints, B-29, at the top and knuckle joints, GC-92, at the bottom. The original ball joints are not available but these,


which are a pretty good approximation, can be bought on eBay for 15 GBP for 4! The GC-92 parts can also be bought on eBay under the name “clevis fork yoke end”. These parts, together with making new threaded rods, replace the entire linkage connecting the gearbox and the positive stop and avoids any problems with gear selection arising from worn out parts.

Having copied pawls that were longer than the originals it was not surprising that the new pawls were too long for the original ratchet levers. The picture below shows the pawls in the 2nd gear position where it can be seen that the one on the right does not engage with the notch.


Surprisingly, the longer pawls also didn’t fit in the new Australian manufactured GC-22 ratchet lever, again confirming that although the Aussie positive stop was the same in principle it had been completely redesigned in detail.

By removing 0.010” at a time from both pawls they fitted perfectly.

I found it important that adjustments are made, half a turn at a time, to the length of the connecting adjuster to test the gear selection and after a few iterations I managed to get perfect selection of all gears. It’s quite satisfying when it eventually works! …at least with the bike on the bench.

The pawls were then heat treated. I’ve described what I do for heat treatment in previous blog posts so won’t repeat it here.

The last little detail was to make a new cover plate, GC-33, for one of the positive stops to replace one that had rotted through.

It's not necessary to make these aluminium discs - they can be bought on eBay for a couple of pounds. 

 

Final Drive Sprockets – SL-91

The last job on refurbishing the gearboxes was to replace 2 of the final drive sprockets. These go under the Velo part number SL-91/X where “X” determines the number of teeth.

I had this collection of used sprockets.


Superficially, they might look OK but that’s only because I’ve cleaned them up and put them in the tumbler overnight. Apart from the number of teeth, there is one fundamental difference between them and that is the “insertion length” or depth of engagement of the sprocket onto the gearbox mainshaft. If you compare the depth of slots indicated by the red and blue arrows it can clearly be seen that the red one is much deeper – twice as deep in fact. I found that both of these fit perfectly onto my gearbox mainshafts and so one has to ask the question why use 1/8” of engagement rather than ¼ “? (I actually measured 0.265”).

I found the same characteristic in those available for sale and as I saw no reason to use the shorter engagement depth (or, conversely, I would consider the longer variant to be a better design), I opted to make new sprockets with the greater depth.

The starting point is 2x duplex sprockets with 21 teeth, pictured below with the worn out one to be copied.


These duplex sprockets are made of EN8 steel – quite tough enough for this application and are pretty good value at 25 GBP for 2, including postage. The first step was to hold the sprocket on the hub in the lathe, remove one set of teeth and form the small hub that will go onto the mainshaft.

The sprocket was then turned round and the entire large hub removed, creating a workshop full of cutting oil smoke and a small mountain of swarf in the process.

After repeating the lathe work for the 2nd sprocket


they were set up in the rotary indexer on the milling machine to machine the slots


and drill the ¼” holes for the adjuster peg.

Incidentally, it would not be so easy to setup the sprockets on-centre in the chuck of the rotary table if they didn’t have a number-of-teeth that was divisible by 3.

After chemical blacking


they are now fitted to the gearboxes of KTTs 55 and 305.


And that’s about it for gearboxes, clutches, positive stops etc. About 4 months of work in total.

In fact, that’s about it for this year. As soon as the effects of Christmas have worn off, the grandchildren have gone back to their homes to play with their new toys and, hopefully, Father Christmas will have deposited a 4-axis CNC machine into my Christmas stocking it will be time to get back in the workshop and start work on the engines.

In the meantime,

Happy Christmas

 


Wednesday, 4 December 2024

4-Speed Gearbox for the Velocette Cammy Special

I have so far rebuilt 4 early Velo 3-speed gearboxes – those for KTT 55, KTT 305 and 2 flat-tankers. I had one last gearbox to prepare for all 5 Velo projects and this was my one-and-only 4-speed ‘box. It’s marked as #2 in the picture below.


I bought this ‘box many years ago and it was advertised as being rebuilt and in good condition. Superficially it looks fine and all the gears selected positively, however, I have learned never to take these assurances at face value. So, off with the cover to see how it looked inside.

Pretty good. Bearings had been renewed, teeth and dogs on the gears were good, there was a small repair to one of the lugs on the front but I would consider this gearbox to be in excellent condition and did not require any attention inside.

However, there is always something to do! When the positive stop was fitted it was immediately apparent that the “Outside Striking Lever” (Velocette parts book terminology), part number BK-65/3, that was fitted was wrong.


There are 2 fundamental differences In comparison to the B-65 component on the 3 speed gearboxes: BK-65/3 has a spline fitting rather than a square and it is 1” shorter. The lever that should be fitted is an earlier BK-65 that has the same spline but is longer.

I didn’t have a correct BK-65 lever but, luckily, there is an easy solution: add a 1” extension piece


made from a tough steel, EN24T, threaded internally and that positions the linkage to the positive stop in the correct place.


The only other part that I had to make was the cable adjuster for the clutch, CK-21, that screws into the top


by copying one from one of the other gearboxes. This, I found, had another weird thread of 19 TPI (the other one was the oil filler that I had to make, see here, with 13 TPI) which I cannot find on any thread chart for this diameter. Luckily, my 76 year old Harrison lathe can cut these obscure threads.

On the clutch side of the gearbox, a new thrust bearing and the wire clip for the thrust cup, BK-52, were replaced.


I have found on 2 of the gearboxes that I have rebuilt that the back of the clutch has contacted the wire clip and this had ground a flat on the wire – in one case it had nearly severed it into 2 pieces.

I have not yet decided what chaincase to fit but in the meantime, I have lock-wired the 4 screws that would fix the chaincase to the gearbox.

One of the 7-plate clutches that I rebuilt was fitted with new C6/2 Thrust Pins

and 16 new clutch springs

before putting on the sleeve gear nut with a new C8 washer.

All 5 gearboxes that I need - 3 for the immediate Velo projects and the 2 that I plan to work on subsequently, have now been rebuilt.

There are a couple of minor things to finish off but, essentially, this part of the project is complete. This particular gearbox is now in the bike.

This is the pile of bits that has been replaced (and there are a few more parts already in the bin) from the gearbox rebuilds.


Before moving on to the next part of the “transmissions sub- project” (which is to get 3 working positive stops) I should mention that it is essential to have a few special Velo tools to assemble and adjust the clutches, shown below.

Without these, it is pretty well impossible to set up a Velo clutch. I acquired these many years ago for my Venom and Thruxton ….not much changed from the 1920s to 1971.

I also have a lot of clutch parts left over.


If you want any of these bits then let me know (email address at top right of page) as I have no further use for them. There are some 3-plate clutches in this pile of bits. Ideally collect from my home close to Worthing, West Sussex or I can bring to a Kempton autojumble, Founders Day or the Banbury Run in 2025.

There is also a complete set of standard ratio gears in good condition available that I replaced with a CR set in KTT 305s gearbox.


 

And finally…..

For those of you that are members of the Velocette Owners Club and that read the clubs magazine, Fishtail, you will be aware that there has recently been a series of concise and well-written articles by Brian Agnew about flow and combustion in engines.

I spent 40+ years of my working life engaged in exactly this topic, namely developing, validating by way of experiment and applying Computational Fluid Dynamics software for in-cylinder flow, fuel injection and combustion in the design and development of IC engines. In his most recent article (Fishtail 504) Brian refers to “Barrel Swirl”, more often referred to in the industry as “Tumble” – flow rotation about an axis parallel to the crankshaft. To illustrate this, I poked around in some old directories on my PC and found an animation of an in-cylinder flow calculation for a modern 4-valve engine (well, reasonably modern – I retired 9 years ago) which I have shown below. The surfaces of the intake and exhaust ports with the piston at TDC in the cylinder look like this:

and the flow generated during the intake and compression strokes are shown in the animation below.


The flow structure in earlier designs of 4-valve engines, such as the Rudge, would be completely different. Intake ports in modern engines are designed to achieve separation as the flow enters the cylinder to generate the rotation, seen in the above animation. The rotational speed increases as the air is compressed during the compression stroke (conservation of angular momentum - spinning ice skaters decreasing their moment of inertia by moving their arms inwards) and dissipates into small-scale turbulence as the piston approaches TDC. As Brian mentioned in his article, it is the small-scale turbulence that determines the turbulent burning velocity - the speed that the flame propagates; without these processes engines simply wouldn't work.

Such calculations were carried out routinely for competing designs, more often with fuel injection to assess fuel-air mixing, in the R&D departments of major manufacturers. Whether that is still the case I doubt very much ...the engineers that I used to work with are now either working on electric vehicles or pensioned off.

 

Saturday, 23 November 2024

Rebuilding a Model K Gearbox, an Alternative Hand Shift and my First Motorcycles

 

This is the last, the 4th in fact, of the early 3-speed gearboxes that I have rebuilt.

This one is from an early Model K and has a very interesting hand shift attached directly to the gearbox rather than the usual petrol tank mounted lever.


As some of the bracketry and the gear change lever itself is remarkably similar to that found on the later positive stop mechanisms my initial reaction was that this is an early (discarded prototype?) positive stop. However, looking at it a bit closer it is not a positive stop – there is nothing in the mechanism to prevent a 1st to 3rd gear change; it is simply an external gate and fulfils the same function as the GC-3K Gear Control Gate that would have been a factory fitting. Why has it been fitted instead of the production item? I have no idea …like so much else, it is lost in the mists of time.

The one observation that I can make, however, is that quite a bit of effort has gone into making it. I don’t believe that it originated from the Velocette works at Hall Green but it could have been made in the workshop of one of the main Velo dealers, L. Stevens Ltd. in London, to whom the bike was shipped in 1926. In spite of the corrosion on the ferrous components, the gear change turned out to be quite serviceable – many of the nuts/bolts/screws were brass, which helped. Anyway, more about this later.

The gearbox was in remarkably good condition with no bits broken off, good threads throughout and with just the usual wear and tear of the internal components that would be expected after nearly 100 years.

On stripping the gearbox, I was surprised to find that it was fitted with a close ratio gear cluster.

There is a bit of rounding on the teeth of the mainshaft 2nd gear but quite serviceable. The fit of the bush in the sleeve gear was not so good - it was free to rotate, but the wear of the bush on the surface with the mainshaft was quite acceptable and, after aligning the oil holes, a thin coating of Loctite 638 will ensure that the sleeve gear bush never moves again.

The clutch operating lever, C-31/2, that bears on the ¼” diameter thrust pin was not in quite the right place, as evidenced by the witness marks,

and this could only be corrected by removing a small amount of material from deep inside the gearbox shell using a Dremel at the location indicated with a bit of welding rod in the picture below.

The operating lever now bears centrally on the pin.

The layshaft end float was checked in the same way as the other gearboxes (see previous blogs) and a 0.011” shim was added behind the B-22/3 bearing to adjust to 0.008”.

On stripping the gearbox, I found that a 0.080” brass spacer had been placed between the sleeve gear and the bearing

and when I checked the meshing of the sleeve gear and layshaft gear I found that the alignment was perfect. Clearly, someone had taken the trouble to build this gearbox carefully in the past.

All bearings, including the sleeve gear bearing, were renewed - 4 in total. Finally, I found that the B3 cap that screws into the end cover did not quite reach the outer of the bearing that supports the end of the mainshaft resulting in the bearing being not properly clamped. A small annular disc was therefore made to ensure the bearing is locked in place.

Now, back to the external gear shift mechanism. The picture below shows the complete mechanism after removal from the gearbox.

After stripping, grit blasting the larger parts and putting smaller parts in the tumbler overnight, the various components cleaned up well.

It is impossible to get rid of the corrosion but all of the ferrous parts are serviceable and were subsequently chemically blacked before reassembly.

But first, a few observations about this mechanism: first and foremost, it is not a positive stop mechanism. The spring-loaded pawl and cam (the bit with the notches) replicate the functionality of the B64 “gear striking selector” (Velo parts book terminology) and the B66 selector plunger that are located inside the gearbox, shown below.


(note: the above picture is from one of the other gearboxes – the only difference is that this gearbox did not have the notch for neutral)

The second observation is that there are 2 sets of notches. One set has 4 notches – 3 deep and one shallow (and similar to the setup in the above picture) and at the other end are 2 notches for the pawl to engage.


As it was set up, the pawl engaged with the 2-notch end rather than the 4-notch end. Why would that be when there are 3 gears and a neutral? The semi-circular cam part could be fitted either way round and so the only way to find out was to try the 4-notch end.


The reason immediately became apparent: the notch for 2nd gear had been put in the wrong place! By checking the distance (to ensure it is the same) between the B65 striking lever and the point of connection of the linkage on this mechanism in each gear I found that 1st, 3rd and neutral were correct whereas the notch for 2nd gear should have been in the position indicated by the mark that I engraved on the cam shown below.


Whoever made it assumed that the notch positions for 1st, 2nd and 3rd would be equidistant – they are not. Rather than make another cam, they simply swapped it around, made 2 notches for 1st and 2nd and 3rd would be selected without a notch – this works fine – I’ve tried it.

If I can find a spare day or two, I’ll make another cam with 4 notches and try and get them all in the correct places.

In the meantime, the gearbox and the shift mechanism are all reassembled and working well. The gear indexer may not be pretty but it is an original period feature, probably made 95 years ago, and is part of the provenance of this bike.



I’ll make a new ¼” threaded adjuster rod and refit the kickstart in the next day or so.

 

And Finally….

Somebody asked me recently what was my first motorbike. Well, the first motorbike that I rode legally on the road at the age of 16, back in 1967, was an AJS Model 20 with a Swallow single-seat sports sidecar. The AJS Model 20 is a 500cc twin. In those days, the law allowed learners to ride solo motorcycles up to 250cc and unlimited (!!) capacity if a sidecar was fitted. I went for the 2nd option. Life was much simpler then: a new rider applied for a provisional driving licence, bought insurance and off you went on the steed of your choice – without any training whatsoever.

By the way, please don’t think that this bike was in any way exotic. I bought it from a mate for 5 GBP and it subsequently needed a lot of work to make it roadworthy. I had also never ridden a bike + sidecar before and anyone that has previously ridden only solo motorcycles gets the shock of their life the first time they ride a combo! As you quickly find out, you have to steer them and point them where you want to go rather than leaning.

Anyway, in those days I lived in Shanklin in the Isle of Wight and on the day of my 16th birthday I set off from the farm from where I had bought the bike to a motorcycle dealer in Carisbrooke by the name of Dave Death to get an MOT. They are still in business now – see their website here. If you scroll down their web page you will see a picture from 1962 – this is exactly how it looked when I went there.

The bike failed it’s MOT test on pretty well everything and so I set off for home – it’s about 10 miles - to start repairing things. About half way home, just coming into a village called Godshill, I was approaching a left hand corner and blipped the throttle to change down a gear and ….the throttle stuck wide open. There is nothing worse than an engine revving it’s nuts off under zero load – there was no kill button and the only thing to do was to keep it in gear and try and slow it down. Anyone that has ridden a sidecar outfit knows only too well the consequence of too much speed in a left-hand corner: either the sidecar wheel comes off the ground (as a prelude to turning over) or you straighten up, keep the sidecar wheel on the ground and go straight on. I choose the latter and went straight through a hedge on the opposite side of the road, ending up in the middle of a vegetable patch of somebody’s garden ….with the engine still revving. I managed to stop the engine by removing the spark plug caps and simultaneously electrocuting myself. But at least the engine was now quiet. After a bit of work, I nursed it home. An interesting first day on the road.

However, this wasn’t my first ever 2-wheeled + engine “thing”; that was a Velo Solex. For anyone that doesn’t know what these are they look like this.

Acknowledgement to whoever owns the copyright of this picture.

These were produced in prodigious quantities in France immediately after WW2 and consist of a 49cc engine that has a friction drive onto the front tyre. The engine pivots and so can be ridden as a cycle. It is started with the engine lowered, pulling in a decompressor lever with the left hand, pedalling like hell, letting the decompressor lever go ….and away you go. There was no throttle – either the engine is under power or it’s not.

So, how did I come by one of these? Well, back in secondary school days it was customary for boys (I have no idea what girls did – I had zero interest in girls at the age of 13) to get a job during the school summer holidays. I had a variety of jobs during my school years – gardening, clearing tables and washing up for a tearoom, making plastic bags in a factory, working in a garage but the first job that I had, for 3 summers in fact, was working at a shop by the name of Barney’s Emporium in Shanklin.

This is a picture of it in its heyday.

Acknowledgement to whoever owns the copyright of this picture

The shop was interesting, to say the least; it was owned and “managed” by Barney Powell and the part of the business that made any money was selling binoculars and telescopes. The other part of the business was a joke shop and the shop window was full of Barneys own jokes and comical take on life and which raised money for charity which was donated to the local Cottage Hospital each year as I recall.

Barney came from a family of actors/musicians/comedians and Barney himself was a comedian and musician that, among other things, played the xylophone on stage with his feet while sitting on a high stool! Quite a character.

Acknowledgement to whoever owns the copyright of this picture

But back to motorised bicycles…. Barney had a Velo Solex and for the 3 years that I worked for him he asked me to take it to a garage in a nearby town for an MOT test. I was supposed to pedal it there but, needless to say, once I had gone past the local police station in Shanklin I lowered the engine onto the tyre and experienced the pleasure of power for the first time. I remember when I got back (having passed the MOT) Barney feeling the cylinder with his hand and, with a glint in his eye, commenting on how hot the sun was today.

It turned out that this was his second Velo Solex. He had given an older one to a previous employee that had since started work as an engineering apprentice but had no interest in, and had done nothing with, the bike. I acquired it (for nothing) and then started to figure out how to get it to go. The engine on these bikes has a small petrol tank on the right side and a flywheel magneto/lighting coils on the left. After fiddling around, not really knowing what I was doing, I managed to get it going.

In the meantime, I had spotted another little bike with an engine in my neighbours open shed in their back garden. It had been there quite a few years, quietly rotting away, and I got this one too. It was a Cyclemaster – one of these.

Acknowledgement to Bonhams

I managed to get this going – so now I had 2! And what do you do when you have 2? You race them. There were always plenty of quiet lanes and footpaths where my buddy and I could ride these – we were still some years away from 16 years of age - we’d end up in some kind of social care these days. But it was pretty harmless and we learned a lot.

So which bike won? The Velo Solex. Although I didn’t know this at the time, the Cyclemaster was produced in 2 engine sizes: initially 25.7cc which was increased to 32.6cc in 1952. Although mine had the larger engine it could barely power a skinny lad along a straight – it was one of the noisiest and definitely the most gutless bike I’ve ever ridden.