I needed 3 positive stops for the 3 immediate projects – KTT 55, KTT 305 and the Cammy Special. Both KTTs have a 3-speed gearbox and the cammy special will use the 4-speed ‘box.
This is the collection of positive stops and assorted parts that I have.
The one on the top right of the picture is a new-manufactured item that I bought on eBay Australia many years ago and is the only one that I have that will fit the 4-speed ‘box. The backplate, GC-2/2, is different for the 3 and 4-speed gearboxes – the top central hole is in a different place, although I could only find one part number in the spares book.
The other 2 complete positive stops are from KTT 55 and KTT 305. The latter has the wrong mounting bracket but luckily there is a correct bracket in the collection of bits at the bottom of the picture.
The new positive stop had been expertly crafted – a real work of art and superbly manufactured. This, for example is one of the pawls.
And this is the motley assortment of pawls from my old positive stops
and which were all pretty loose in their holes in the main body, GC-21 (referred to as the “Centre Piece” in the spares book – makes it sound like a floral table decoration for a dinner party!).
I decided that I would make some new pawls by copying the new ones that had come from Australia. These need to be hardened steel and so the first step was to order a bar of O1 tool steel of an appropriate size that I could subsequently heat treat.
I then chopped a piece off and after cleaning up the ends, set it up in the 4-jaw chuck in the lathe to machine the spindle.
The nominal ¼” diameter (actually 0.245”) spindle on both the Aussie pawls and my copies is slightly longer than the originals and as the longer spindle fits into my GC-21 main bodies, I retained this feature because I believe it is a better design as the pawl is better supported.
After measuring the angle of the tapered surfaces with a digital protractor
The pawl was set up in the rotary indexer in the milling machine to complete the machining.
After a few hours I had 2 new pairs of pawls – Aussie new ones on the left in the picture below.
These pawls turned out to be longer than the originals that were part of the 3-speed positive stops – 0.82” versus ~0.78”. While I was making these, I compared a few other parts of the new positive stop with the originals. Interestingly, I found that the 3-speed ratchet lever, GC-22, was different: the picture below shows the new Australian manufactured one on top of an original.
I concluded that whoever made this in Australia redesigned much of the mechanism. Anyway, with the 4-speed ratchet lever fitted, it worked perfectly on the 4-speed gearbox with positive selection of all gears and neutral.
So, back to the 3-speed positive stops.
Before fitting and testing the new pawls, I needed to sort out 2 new linkages that connect the ratchet lever to the Striking Lever, B-65. I believe that I mentioned in the past about the importance of eliminating any sloppiness through wear in the linkage on hand-change vintage Nortons using Sturmey Archer gearboxes – it invariably results in difficulty in selecting or staying in gear. When rebuilding these Velo gearboxes I had found on all of them that the part referred to as the ”striking lever double knuckle joint”, B-69, was badly worn and introduced a lot of free play and I replaced all of mine. This part is (or, at least was) available from Grove Classics.
I also replaced the rest of the linkage: new ball joints, B-29, at the top and knuckle joints, GC-92, at the bottom. The original ball joints are not available but these,
which are a pretty good approximation, can be bought on eBay for 15 GBP for 4! The GC-92 parts can also be bought on eBay under the name “clevis fork yoke end”. These parts, together with making new threaded rods, replace the entire linkage connecting the gearbox and the positive stop and avoids any problems with gear selection arising from worn out parts.
Having copied pawls that were longer than the originals it was not surprising that the new pawls were too long for the original ratchet levers. The picture below shows the pawls in the 2nd gear position where it can be seen that the one on the right does not engage with the notch.
Surprisingly, the longer pawls also didn’t fit in the new Australian manufactured GC-22 ratchet lever, again confirming that although the Aussie positive stop was the same in principle it had been completely redesigned in detail.
By removing 0.010” at a time from both pawls they fitted perfectly.
I found it important that adjustments are made, half a turn at a time, to the length of the connecting adjuster to test the gear selection and after a few iterations I managed to get perfect selection of all gears. It’s quite satisfying when it eventually works! …at least with the bike on the bench.
The pawls were then heat treated. I’ve described what I do for heat treatment in previous blog posts so won’t repeat it here.
The last little detail was to make a new cover plate, GC-33, for one of the positive stops to replace one that had rotted through.
It's not necessary to make these aluminium discs - they can be bought on eBay for a couple of pounds.
Final Drive Sprockets – SL-91
The last job on refurbishing the gearboxes was to replace 2 of the final drive sprockets. These go under the Velo part number SL-91/X where “X” determines the number of teeth.
I had this collection of used sprockets.
Superficially, they might look OK but that’s only because I’ve cleaned them up and put them in the tumbler overnight. Apart from the number of teeth, there is one fundamental difference between them and that is the “insertion length” or depth of engagement of the sprocket onto the gearbox mainshaft. If you compare the depth of slots indicated by the red and blue arrows it can clearly be seen that the red one is much deeper – twice as deep in fact. I found that both of these fit perfectly onto my gearbox mainshafts and so one has to ask the question why use 1/8” of engagement rather than ¼ “? (I actually measured 0.265”).
I found the same characteristic in those available for sale and as I saw no reason to use the shorter engagement depth (or, conversely, I would consider the longer variant to be a better design), I opted to make new sprockets with the greater depth.
The starting point is 2x duplex sprockets with 21 teeth, pictured below with the worn out one to be copied.
These duplex sprockets are made of EN8 steel – quite tough enough for this application and are pretty good value at 25 GBP for 2, including postage. The first step was to hold the sprocket on the hub in the lathe, remove one set of teeth and form the small hub that will go onto the mainshaft.
The sprocket was then turned round and the entire large hub removed, creating a workshop full of cutting oil smoke and a small mountain of swarf in the process.
After repeating the lathe work for the 2nd sprocket
they were set up in the rotary indexer on the milling machine to machine the slots
and drill the ¼” holes for the adjuster peg.
Incidentally, it would not be so easy to setup the sprockets on-centre in the chuck of the rotary table if they didn’t have a number-of-teeth that was divisible by 3.
After chemical blacking
they are now fitted to the gearboxes of KTTs 55 and 305.
And that’s about it for gearboxes, clutches, positive stops etc. About 4 months of work in total.
In fact, that’s about it for this year. As soon as the effects of Christmas have worn off, the grandchildren have gone back to their homes to play with their new toys and, hopefully, Father Christmas will have deposited a 4-axis CNC machine into my Christmas stocking it will be time to get back in the workshop and start work on the engines.
In the meantime,
Happy Christmas